Original schematic L1 & L2 shows 2 x 52.5mh in series, 105mh. Looks to be ferrite pot core types. The AC PCB only uses one ~ 50mh, instead of two at 105mh combined.
Any comments on these Wilco shielded inductors for L1 & L2 ~50mh and L3 (R38/100r) 12uh. Notes on side indicate not suitable for DC apps, due to low saturation.
Having trouble finding caps locally with correct lead spacing to fit the PCB. specifically the 150uf / 50v .
A option for less costly part MMBT3640 (sot 23, 3 leg) footprint to allow PN3640 pad flexibility , since TO-92 PN3640 is obsolete and pricey part. Possible Alternative to PN3640 (TR11) : MPS3640, 2N4209 (15v Ic 50ma ? ) , 2N5771 (15v, Ic 200ma ) , MPS5771 ( 15v Ic 50ma ?) Not sure what the min Ic current req should be , PN3640 is 200ma, and if 12v vs 15v Vce makes any real difference. If not maybe a 2N3906 or 2N4403. The PN3640 is a high speed switch , not sure if a general purpose PNP with similar Vce and Ic would work instead.
Would be nice to have a toroid or pot core inductor specified for the osc board as a alternative to the TLC555 chip to keep the design as close to original. Ex: wire # , core part number description (ferrite or permalloy) and wire turns starting point are unknown leaving TLC555 chip the only option , the cost on the chip is reasonable though. Should'nt be to hard to experiment with toroid cores and windings to get close. The one pictured ( T3 80uh ) is a small one for the oscillator board. Not sure if 80uh is accurate though. Time to gather some cores and wire for some experiments. It looks as if its a easy wind at around 3-4 turns.
